MTA launch, 2020-07-25

by Dave Nordling, RRS.ORG


On July 25, 2020, the Reaction Research Society held its first launch event at the RRS MTA since the start of the pandemic. Our pyrotechnic operator in charge that day was our society president, Osvaldo Tarditti. I was his backup. We also had Jim Gross come out for the event who has been our pyro-op in charge at many of these events.

We observed social distancing as best as we could and everyone was wearing a mask. Protective equipment is normally required for loading operations and keeping our people spread apart only makes good sense. The heat (107 F) was significant but everyone was largely prepared to endure the exhausting environment. We had a few glitches in the launch process which can happen at any event. It is times like these that make patience and planning very valuable.

We held a short safety briefing before beginning launch operations. I reviewed the natural and man-made hazards at the MTA, underscored the importance of hydration, the buddy system and montioring each other and ourselves for hest exhaustion. We had a lower turnout as this was a private society event and with the heat we sought to run through the micrograin launches in one straight series holding the hybrid rocket flight for last. After the safety briefing, Larry performed a propellant burn demonstrstion then we adjourned to the observation bunker while the pyro-op’s began to ready the micrograin rockets in the rack. John Krell assisted me with the rack loading and arming process.

We had four micrograin rockets and the hybrid rocket for this launch event. There were three alpha rockets with slight differences in their design. John Krell had built three avionics payloads, one for each, to capture the trajectory data (acceleration and barometric pressure) so that an apt comparison could be made. We also had an avionics package and recovery sytem (parachute) built into the beta by Jerremy Hoffing, son of Larry Hoffing. The hybrid rocket would be last in the series,

Bill Inman surveys the upper half of his launch rail made from electrical conduit for the three-finned steam rocket he built.

Bill Inman came to the launch event to both spectate the launch of the micrograin and hybrid rockets and also examine portions of his launch rail unit from his Scalded Cat steam rocket project. He has already begun planning a newer steam rocket design.

Bill Inman captures a launch from his cell phone camera from the MTa observation bunker.

THREE ALPHAS

This segment talks about the three alphas we built and flew to compare two design changes. The three designs were:

  • standard alpha with three-foot propellant tube, plain carbon steel nozzle
  • standard alpha with three-foot propellant tube. ceramic coated nozzle
  • longer alpha with four-foot propellant tube, ceramic coated nozzle

Among these three designs, we were examining the effect of the ceramic coated nozzles which used a proprietary coating process used on automotive engine pistons and exhaust pipe interiors in the racing industry. Specialized Coatings was the company providing the service which we have used before. The coating was proven in a prior alpha flight in 2017, but the nozzle was misplaced and lost after photos were taken at the event. A repeat test was warranted to not only provide photographic evidence but also to cut-up a nozzle to see how the coating survived. It is likely that a ceramic coated nozzle can survive multiple firings before erosion sets in.

Converging part of an alpha nozzle with the ceramic coating
Diverging part of the alpha nozzle with a ceramic coating.

The other variable explored was to change the length of the propellant tube and thus increasing the propellant available. Past projects have explored using longer propellant tubes, but this project would bring flight data for direct comparison. To achieve maximum altitude, a second ceramic coated nozzle was used. Just based on the time of flight observed from the observation bunker, the four foot alpha remained aloft for at least four more seconds. John Krell took some video like a few others did. We may be able to estimate the trajectories if we fail to recover the data from one or all of the alphas.

The four foot alpha rocket payload is being loaded.
The four foot alpha rocket sits in the alpha rails with the beta rocket in its own rail launcher behind it.

BETA WITH RECOVERY SYSTEM

The beta rocket used at the launch event had a recovered nozzle which had some minor erosion. This was sufficient for this flight. The two features were the parachute recovery system and the avionics package to record altitude data.

Beta rocket with a classic Dosa-style fin can.

The beta was the first micrograin rocket ready for flight and thus it was loaded into the box rails built for the beta. This beta design differed from the standard design by having a straight coupler meaning that the aluminum payload tube was the 2.0-inch diameter as the 2.0-inch DOM steel propellant tube. Because of cost, betas are produced in smaller and less frequent batches. This sometimes leads to more variations in the design. With a little more part production, we can achieve greater consistency between betas.

The used beta nozzle sits next to the Dosa-style fin can

The typical aluminum coupler design flares out to a 2.5-inch aluminum payload tube. The standard design better fits the box rail launcher which was made with a 2.5-inch bore. The standard payload tube size would have offered more room for packaging the recovery system. Nonetheless, Jeremy was able to fit everything together and the beta propellant tube was filled and made ready.

The 2.0-inch rocket did lay properly inside of the quad-rail launcher, but the sloppy fit was a little concerning. We had considered using a sabot to fill in the gap, but no practical solution could be made. The solid steel rails would contain the rocket but the concern was whether the avionics switch would get bumped into the off-position. To avoid this, a small block of wood was used to lift the beta high enough to clear the switch near the top of the payload.

The ignition wiring of the beta with the dual igniters is rechecked by Osvaldo. The beta is propped up on a chunk of wood to clear the payload switch. There was a concern that it could accidentally switch off.

The first launch attempts resulted in no firing. After re-checking the cabling and my hookups, no error was found. Second attempt also had the same negative result. To expedite the launch process we proceeded with the alpha launches.

The beta under repair in the old blockhouse.
Two burst disks with two electric matches.

After the alphas flew, we re-tried the beta rocket with a dual-igniter for redundancy, the first electric match was found to be defective. This time after some initial trouble with the battery, on the third attempt we got ignition.

Still capture of the beta rocket at the 7/25/2020 launch event
A massive smoke plume from the beta just a fraction of a second after ignition

SECOND FLIGHT OF THE HYBRID ROCKET

A new rocket body was built to hold the same Contrails H222 nitrous oxide hybrid motor flown earlier. this year. Larry Hoffing did a lot of work building a new rocket body from scratch. It’s boat tail was fitted to accept the 16-inch long, 38mm casing of the Contrails H222 model. Osvaldo built in the parachute recovery system and all parts of the rocket fit well together at the RRS MTA. I changed the location of the vent tube and routed the line to the outside trimming the excess away once the rocket was vertical and captured in the 1010 rail. A lot of this preparation was documented on the RRS Instagram page.

The second fllight of the hybrid rocket sits on the 1010 rail.
The hybrid rocket sits on the 1010 rail positioned for flight

The Contrails H222 motor is a very simple design made for reloading and re-use. The designs are built to common metric standards used in model rocketry. Using the smallest size, 38mm, for a first hybrid project made sense as we would learn the practical things necessary for a successful launch. It also was a size very close to the micrograin rockets that the RRS commonly uses.

The Contrails H222 motor slipped into the rocket body awaiting the retaining ring. The igniter is taped against the nylon filling line going up the nozzle, fuel grain and up to the floating injector fitting.

The Contrails design is very simple and easy to assemble with the right tools and lubricants. The interior of the 16-inch long motor is divided into two parts, one for filling with nitrous oxide liquid supplied under pressure and the other holds the inert plastic reloadable fuel propellant grains and a graphite nozzle. The two volumes are separated by a dual O-ring sealed piston called the floating injector.

Cross-sectional illustration of the Contrails hybrid rocket motor

The motor uses a snap-ring retention method for securing the graphite nozzle plug in the aft and another snap ring is used to keep the vented top plug in place. The internal pressure of the nitrous oxide liquid holds the floating injector down against the fuel grain. The injector consists of a stainless steel Parker push-to-connect plastic tube fitting. The ignier is designed to break the filling line inside of the motor releasing the flow of nitrous oxide and providing ignition nergy to start the combustion of the plastic fuel grain in the presence of newly streaming oxidizer flow. It is a very simple and impressive system. Contrails also sells kits and replacement parts to replace those that wear out.

Top bulkhead fitting with an orificed vent line in the top, snap ring is installed and removed with a special tool.

Last launch attempt successfully demonstrated the motor assembly, motor integration into our first rocket body and loading process. The remote actuation of the nitrous filling line and separate electric ignition circuit required a two-channel firing rig which operated well as expected. The flaw in the first aunch was failing to quickly and cleanly sever the thick-walled nylon fill line.

The floating injector with the 3/16-inch nylon fill line inserted. The Parker brand push-to-connect fittings are used for this application.

The nitrous bottle was recharged with liquid and secured to an I-beam. The valve manifold was attached and after a quick tightening was free of leaks. We secured the electrical and fluid connections to the rocket and ran our control lines back to the old blockhouse with all of our observers in the safety of the observation bunker. Osvaldo and I conducted all operations with care. Then the first problem struck.

Nitrous bottle with the filling manifold

We couldn’t get the fill solenoid to open. This was first thought to be the battery. In past summer events the heat can degrade the battery. We had several no-fire conditions which led us to suspect the battery health. For the beta, the fault was a broken lead on the electric match. Running a voltmeter showed a little weakness of the battery but 12-volts was showing on the needle. We moved one of the cars closer to the blockhouse to use its battery but the solenoid still wouldn’t open. Given, the late hour in the peak of the afternoon, we scrubbed the launch attempt and safed and disconnected the fluid and electrical system.

Nitrous oxide bottle courtesy of Nitrous Supply Inc. in Huntington Beach. The fill-drain system with remote operated solenoid valve.

The bottle pressure was reading very high that day and although the vessel and plumbing is amply rated for the 1400 psi reading on the gauge. By weight, the bottle wasn’t overfilled, but the heat of the day certainly brought the pressure up. The solenoid valve was bought as part of an assembly sold by a different supplier. With no labelling or marking on the solenoid, there is nothing to identify the manufacturer or model number. A couple emails were sent to the seller but no information on the valve make and model has been given. The internal design and operating limitations of this 12 VDC normally closed solenoid valva is unknown but it is possible that the high pressure against the seat was too much for the solenoid to overcome. Chilling the bottle or simply venting the bottle to lower the pressure might have helped. More tests of the solenoid valve will be done to verify its functions and perhaps some careful disaasembly of the valve may reveal markings to identify it. We are also considering building our own simple solenoid valve fill and drain assembly once the right parts can be specified.

IN CLOSING

It was a long day but very worthwhile. We hope to have another launch event soon. The results of the day’s events will be discussed at the August 14, 2020, monthly meeting which will be held by teleconference.

Lovking up the gate at the end of the day.

MTA launch, 2020-03-01

by Dave Nordling, RRS.ORG


The RRS held a launch event on Sunday, March 1st, 2020, at the Mojave Test Area.  It was a brisk morning with steady winds that occasionally slowed enough for a safe launch.

This launch event was originally for a university static fire and a few member projects.  The university had to reschedule but we had sufficient interest from our own projects so we held the event.

View from behind the RRS MTA large test stand, 2020-03-01

The weather was a concern with passing storms and rain predicted earlier in the week.  But as often happens, the weather shifted for the better on launch day with winds staying low enough to launch most of our projects.

Wolfram’s booster sits on its stand in the Dosa Building

Wolfram has been working for a few years on his Gas Guzzler ramjet rocket. He is just now entering the first system flight tests to demonstrate the staging and recovery systems.  He filled his ramjet with water in place of the gasoline to have a representative weight.

The Gas GUzzler booster stage on the 1515 rails, loaded and ready
Both stages of the Gas Guzzler sit on the 1515 rails as Wolfram inspects the fit between them

Wolfram was able to load his booster on to the 1515 rails with good alignment. His upper stage had some alignment problems due to using a different prototype for this initial flight.  After some examinations on the pad, he pulled his rocket stages back to the Dosa building for internal adjustments to assure a clean fit between the booster and upper stage.

Kieth Yoerg’s rocket, Charlie Horse is made ready for flight from the 1010 rail
Charlie Horse rises on the black plume of a Smoky Sam high-powered motor.

The next launch was Keith Yoerg’s high powered rocket, Charlie Horse.  He used an I-350 Smoky Sam motor and had a dual-deployment system with a GPS tracker built in.  The flight was smooth off the rails but the trajectory data seemed to show a steady wind pushing west to east. He reached an apogee of around 4000 feet. Recovery wasn’t a problem as his rocket landed just a hundred yards east of the RRS MTA.

Wolfram stands with his ramjet upper stage and its broken cowl piece. Some rework will be required.

Wolfram returned his rocket to the pad but accidentally dropped the second stage breaking a piece of the ramjet plastic cowl on the concrete below.  With this significant disruption of the aerodynamic surface, he was forced to abort the flight and rework this part.  He was also going to check some of the other parts in his assembly for this long-awaited first flight.  It’s important to not rush a project and wait until all is ready for a successful flight.

Osvaldo and Larry check the payload packaging of the hybrid rocket one last time
The hybrid motor is installed and ready for today’s launch.

The next flight was to be the hybrid rocket that Larry, Osvaldo and I have been working. The Contrails H222 motor was safely loaded from last month and after some improvements to the vehicle body for better parachute recovery functions, we felt we were ready.

The winds were still favorable so we proceeded with clearing the area and making our electrical connections back to the old blockhouse.  With just a handful of people and the lightweight vehicle, the old blockhouse was sufficient for our operations that day.

The RRS nitrous oxide bottle ready to fill our hybrid rocket motor

The nitrous bottle was refilled from the prior week and the manifold was plumbed to the vehicle tank.  With the opening of the nitrous bottle, remote operations could begin.  The time of tanking the small 38mm H-motor tank was not precisely known, but was not expected to take very long given basic calculations of the available flow rate.  As expected, the tank volume primed within 15-20 seconds.  We waited a full minute as we were initially unsure of whether the full volume was filled with liquid.  After spotting a jet of liquid escaping from the vehicle body vent, we were assured that the hybrid motor was ready to be ignited. 

Osvaldo conducted the firing operation after a short five-count. The resistor and Pyrodex charge ignited after a slight delay for the resistor to heat up sufficiently. The motor seemed to reach full thrust quickly and leave the rail as expected from the thrust curves from this commercial motor.

Kieth Yoerg’s onboard camera takes a test photo of me loading the hybrid motor on the 1010 rail

The vehicle was spotted tumbling after leaving the rails leading us to believe the rocket was not properly balanced.  More detailed calculations would have been beneficial, but from initial estimates and the heavier recovery system in the extended rocket body, it was believed the rocket would be stable enough.

Examination of Osvaldo’s high speed camera footage from the hybrid flight revealed the reason for the vehicle tumbling.  Some of the frames show that the nitrous fill line remained attached to the rocket during launch and even after clearing the rails. The fill line did snap loose in the flight at some point, but it was supposed to completely sever at ignition.  This imparted a significant torque to the vehicle leading to a tumbling and short trajectory back to ground.

Note the nylon filling line is still attached as the rocket leaves the rails
Just a little later in the high speed footage the fill line and igniter cable start to come out, but the rocket is already knocked off course.
Both the fill line and cables are free of the rocket while the nitrous still flows over the fuel grain and the motor is lit.

Worse, in my rush to get the hybrid loaded on the rails and made ready for filling operations, I forgot to arm the recovery system.  This is a classic mistake and one that I could have easily avoided. 

At least, the other issues with the flight limited the distance the rocket travelled.  The rocket was recovered just north of the 1010 launch rail still within the bounds of the MTA.  The rocket landed on its nose breaking it and significant body tube damage was sustained. After disassembling the hybrid motor from the body, we opted to scrap the rocket body and rebuild a new one for the next flight.  The fill and fire operations were successful and the equipment we built worked fine.

The first hybrid rocket destroyed in flight. A new rocket build will start soon.
The spent hybrid fuel grain extracted from the Controls H222 motor tube.

The Contrails H222 motor parts survived well. We were able to easily remove the motor assembly and disassembled the parts for inspection. The graphite nozzle showed very little ablation and will be reused.  None of the parts had heat damage.  The fuel grain didn’t exhibit much ablation as compared to the other unburned grains we had. The burn duration in flight seemed to be similar to what is shown on the thrust curve, but this should be reviewed against the flight footage.

More review of the flight footage will be necessary to better understand how the hybrid motor operated. We are considering changing the ignition method to use an electric match and maybe a shape charge that would better ignite the hybrid motor.

We are considering building a static testing rig for the hybrid motor to verify some changes we intend to try with the ignition.  There will be more on this subject in later reports.

Larry holds his experimental solid motor, a simple end burner to test his mixture
Larry suspends his motor from an old steel rod from our modular rail system still under repair

Larry Hoffing had built a custom composite solid rocket motor using a spent casing from a commercial solid motor. This simple end-burner grain also had a custom-made nozzle.  Larry had suspended his experimental motor a length of metal piping threaded on our large adjustable box rails that is still undergoing refurbishment.

Still image from Larry’s motor firing, rapid overpressurization just after ignition

Unfortunately, Larry’s motor design was not successful and rapidly overpressurized scattering both end caps and propellant grain fragments across the desert floor.  No fires resulted from this static firing failure and no serious damage was done to nearby structures used for this demonstration.

Larry’s motor case ripped at both ends, back to the drawing board

The last launch attempt was Keith Yoerg’s smaller model rockets using the tiny B and C motors.  The winds became stronger as the day progressed and by that time sustained wind levels were too high for any launch particularly for such a small vehicle.  These rockets would be saved for a later event and Keith began examining his Charlie Horse rocket and its camera footage.

Kieth’s model rocket launcher being brought back to the Dosa Building as high winds prevented further launches that day.
Tiny desert flowers bloom in the spring at the RRS MTA

It was a good day for the RRS to have a launch event exclusively for our member projects. We plan to hold more of these events for both universities and our membership very soon.


MTA launch, 2020-02-22

by Dave Nordling, RRS.ORG


The Reaction Research Society (RRS) held a launch and static fire event for three UCLA teams and one of our own RRS teams at the Mojave Test Area (MTA) on Saturday, 2/22/2020. Poor weather was a persistent threat from the day before with light rains coming and going from the early morning hours and even throughout the launch day. Winds calmed just enough for a successful rail launch of UCLA’s solid rocket motor. Fortune favors the bold and this proverb did not disappoint our participants that day at the MTA.

Rain clouds still filled the skies on a very calm morning. Preparations began for UCLA’s solid rocket motor launch from our rail.

With the liquid and hybrid rockets, Osvaldo Tarditti, our RRS president was our pyro-op in charge. I served as his apprentice for this event as part of building my experience for becoming a pyrotechnic operator 1st Class. This was the second of two apprenticeships I have served under two first class pyrotechnic operators. Osvaldo gave our safety briefing to all of our attendees that day before beginning the scheduled events.

UCLA gathers around to hear our safety briefing. Most have been to the RRS MTA before but we give the briefing each time to reinforce good practices.

UCLA had three projects ready for flight or static-fire at the MTA. The first was the solid motor driven rocket built by the UCLA Project Prometheus team. They were using a commercial K-sized motor with a vehicle equipped with a downward-facing camera built into the lower body.

UCLA’s Project Prometheus built a rail-launched rocket with a commercial solid motor.
The Gerald Ticonderocket in the color scheme of a common wooden pencil.

Elizabeth, the UCLA team leader for this solid rocket project assisted me with the launch preparations. The rail launched rocket worked perfectly and the recovery system operation was visually confirmed as it descended to the west of our launch site.

My 2-1/2 inch rocket with a commercial H-222 hybrid motor from Contrails Rocketry. The body has been extended for better packaging.
The motor has been successfully loaded into the body tube complete with retainer. All that remains is to complete the recovery system packaging and find our next opportunity to launch.

Larry, Osvaldo and I have made progress on improving the 2-1/2 inch rocket with a commercial H-sized hybrid motor. Larry made an extension on the payload tube to fit all of the recovery system more easily. We have the Contrails H222 motor fully integrated and ready for loading.

The RRS reloaded and refurbished our nitrous bottle and valve manifold, but we didn’t get to loading operations.

Our nitrous bottle was refurbished and reloaded for the testing and we successfully conducted a valve test of the manifold that verified that our control box works well. We were reworking the black powder charge and repacking the parachute when the weather shifted and the winds picked up.

Weather changes quickly in the desert. Our smaller rocket missed our window for launch that day.

The weather was perfect 15 minutes earlier with the launch of UCLA’s solid motor, but at the time we were discussing launch of our hybrid motor it became clear the weather would be getting worse and winds too strong for launch of a smaller rocket such as ours. Since the RRS will be returning to the MTA site on Sunday, March 1. We figured we would do some minor improvements to the payload packaging and try again when we are fully confident and hopefully with better weather for the flight.

The hybrid motor is secured to the RRS I-beam. This is one of the very first assets of the society which predates our arrival to this MTA site.
UCLA hybrid rocket team making load cell adjustments on their thrust stand before hot-fire.

UCLA’s hybrid rocket team under the same name, Project Prometheus, sought to static fire a commercial M-sized hybrid motor as part of getting ready for a flight later this semester. They secured their test stand vertically to our historical I-beam location which was the original article from even before the RRS moved to the current MTA site in 1955. The RRS was glad to assist UCLA in securing to this location and making ready for nitrous oxide fill operations then ignition for static fire measurements.

Hot-fire of the hybrid motor took place around 5pm which by all appearances was a success. The motor case was intact and post-flight assessments looked promising, but an error in data acquisition resulted in no thrust measurements being recorded despite successes in pre-test checkout. UCLA is considering re-attempting this testing at the RRS MTA very soon.

UCLA working on their liquid rocket’s pressurant system.

The last of the three projects would be the static fire of the liquid rocket for Project Ares. The liquid rocket team mounted their hardware to the vertical test stand simultaneously as the hybrid rocket team mounted to the I-beam thrust stand. Both teams worked hard to be ready before the other but in the end, the liquid rocket took longer to be ready.

This would be a second attempt to static fire their liquid rocket system from 2/1/2020 at the RRS MTA. UCLA had been finding and fixing leaks in their pressurization system in the weeks leading before this test.

Making some preliminary checks before commencing liquid oxygen tanking of the rocket.

They proved their fixes before departing to the RRS MTA, but again ran into problems with leakage in the pressurant system. After several more repairs and discussion with the team and pyro-op in charge, the decision was made to proceed. All other systems had passed checks and the leak rates measured were consistent and would only reduce the burn time while assuring safe engine hot-fire.

UCLA begins the final operations following their proven checklist.

Around 5:30pm in the last light of that long day, UCLA’s liquid rocket was proven in a brilliant, steady and powerful hot-fire of their ethanol-LOX propellant liquid rocket. It was an exciting time which showed reasonable thrust results that led UCLA to conclude that the testing that day was sufficient to proceed with flight vehicle integration operations for their motor.

UCLA’s static fire on 02/22/2020 was steady and well controlled.
All initial inspections of the liquid motor looked good. Preliminary review of the data was encouraging and will be useful in grounding their vehicle performance predictions.
In the last rays of daylight, all three UCLA teams pose with their project’s pride at the RRS MTA vertical test stand.

UCLA did a great job of cleaning up at the site. They also returned the LOX dewar back to the nearby Friends of Amateur Rocketry site. We’re thankful to everyone who made this day a triple success. Our next launch event is scheduled for March 1st. We’ll also discuss this and our other recent MTA events at the next RRS meeting on March 13, 2020.