The latest meeting of the Reaction Research Society took place by teleconference on Friday, December 10th and had twelve attendees.
RECAP OF KEITH YOERG’S NOVEMBER LAUNCH OF “THE HAWK”
Keith kicked off the meeting with a recap of the first launch of his rocket “The Hawk” an 8-inch diameter 14-foot tall rocket that was flown from the RRS Mojave Test Area on November 28th. The rocket utilized the 1515 rail launcher which was secured in place to one of the concrete pads using sandbags and tie-downs. The motor was a 98mm Cesaroni M1790 Skidmark which features sparks in the trail.
Keith shared some slow-motion video of the flight captured with a GoPro camera and other data from the flight, including a 3D flight path. The rocket reached an altitude of 4,846 feet as measured by the barometer on the onboard AltusMetrum Telemega flight computer, and was successfully recovered with only minimal damage to the body tube. The rocket is in the process of being prepared for another launch on December 17th to coincide with the anniversary of the Wright Brothers first flight.
RESULTS OF THE 2022RRS EXECUTIVE COUNCIL ELECTIONS
Election chairman Drew Cortopassi presented the results of the 2022 executive council elections. The RRS Executive Council for 2022 is as follows:
President: David Nordling Vice President: Frank Miuccio Secretary: Keith Yoerg Treasurer: Larry Hoffing
The society members in attendance congratulated the incoming new president and other incumbent officers and expressed their gratitude to outgoing president Osvaldo Tarditti for his stewardship of the organization. Osvaldo noted that the future of the group looks bright, and promised to send anyone who asks him a question a photo of him fishing.
USC SOLID ROCKET GRAINS STATIC FIRING
Osvaldo and Dimitri provided a recap of the lengthy solid rocket motor testing campaign that USC conducted at the MTA from December 4-5. On Saturday the 4th, the team worked through the night until around 2 am to be able to complete their goal of firing 20 separate grains of solid fuel by 2:45 pm on Sunday the 5th. The only reported mishap was that the U-Haul the USC team rented broke down just after leaving the dirt road to the MTA, which Dimitri suspected was because they had been using the battery from it to fire the rocket motors.
While the campaign was an ambitious one, the repetitious nature allowed them to get some of the younger students involved who wouldn’t normally be able to take part in on a day when only one motor is being fired. It was remarked that having more young members with hands-on experience is very good for the future of their program and the continuity of knowledge after the upperclassmen graduate. Dimitri mentioned that additional work will be needed to fill in the area of ground blasted away by all the recent USC solid rocket static firings – which has been affectionately named the “Trojan Trench.”
On the same weekend, a team at the FAR launch site launched their “Genesis” rocket – a hypergolic liquid propellant rocket that has been in development since the early 1980’s. Several RRS members had worked on the rocket at various times during its design and fabrication process. Unfortunately, the parachute system did not work and the tanks ruptured on the landing causing a small fire that self-extinguished but was visible from the MTA.
A THANK-YOU FOR DIMITRI’S RECENT WORK AT THE MTA
Our outgoing president, Osvaldo Tarditti, took a moment to extend a special thank you to RRS member Dimitri Timohovich for all of the recent work he has done in improving the facilities we have available at the MTA. Not only did he take the lead in the recent blockhouse roof repair which included several trips up to the site for the initial build, cutting the edges, and installing the tar paper, but he also donated four propane bottles for the society to use in the heaters and BBQ up at the Dosa Building.
In addition, Dimitri has agreed to take on the bulk of the work in building out the interior of the containerized bathroom. Three concrete pads have been poured at the MTA to accommodate this 20-foot high cube container as well as another one adjacent to it.
Osvaldo has procured most of the fixtures for the interior and plans to drop them off at Dimitri’s house – where the container will be delivered so that he can work on it more easily. Dimitri gave a tentative timeline of mid-January 2022 for when the container may be ready for transport out to the MTA.
PLANNING FOR MTA EVENT ON DECEMBER 17
Keith discussed his plans for a second launch of “The Hawk” on Friday, December 17th – this time on a Cesaroni N2600 motor. In addition, Dimitri has an RRS Standard Alpha rocket constructed and ready for launch and Osvaldo agreed to prepare one for Keith to get experience with the Zinc-Sulphur rockets. Dimitri volunteered to bring food for the group – award winning caribou chili made from meat they hunted, dressed, and prepped themselves in Alaska.
CALIFORNIA’S NEWEST ROCKETS CLASS 1 PYROTECHNICS OPERATOR
RRS member Dave Nordling informed the group that he recently learned that he passed his Class 1 Rockets Pyrotechnic Operator’s License exam. Congratulations Dave!
With additional members continuing to work towards earning their licenses, we can make sure that the RRS is able to accommodate a wide range of rocketry testing and schedule requests.
NEXT MONTHLY MEETING
As a reminder – yearly membership dues are due January 1st. Please click on the yellow “Donate” button on the right panel of this website to pay online via PayPal, or mail a check to the society post office box in Los Angeles.
Reaction Research Society; P. O. Box 90933; Los Angeles, California, 90009-0933
The next RRS monthly meeting will be held virtually on Friday, January 14th at 7:30 pm pacific time. Current members will receive an invite via e-mail the week of the meeting. Non-members (or members who have not received recent invites) can request an invitation by sending an email to:
secretary@rrs.org
Please check your spam folders and add secretary@rrs.org to your email whitelist to make sure you are receiving the meeting invitation.
EDITOR’S NOTE: This is a continuation of the reporting from the 10-16-2021 flight of the 6-inch rocket design, built and flown by RRS member, Bill Claybaugh.
This project is part of an effort to develop a two-stage sounding rocket capable of sending about 5 kg of usable payload to about 200 Km altitude. This vehicle is intended to act as the upper stage of that two-stage rocket; it was—based on a systems analysis–sized for an eight second burn-time and about 1300 lbf thrust.
OVERVIEW
As flown the vehicle was 101.25” from nose tip to the fin trailing edges. The Payload section was 40.125” in length and 6.170” in diameter; the booster was 61.125” in length and 6.00” in diameter.
The vehicle had an aluminum nose tip, a filament wound fiberglass nose with a 5.5:1 Von Karmen profile, a filament wound cylindrical payload section, and an aluminum motor / airframe with aluminum fins.
VEHICLE DESCRIPTION
Inspection of the Forward Bulkhead showed it to be in good condition with no evidence of any gas leaks above the two O-rings. The bottom of the Bulkhead showed some damage to the fiberglass heat shield from the ground impact of the rocket but showed plenty of
Pre-flight estimated motor performance was 1350 lbsf. of thrust with a burn-time of 8.35 seconds. Burnout velocity was estimated at Mach 3.1 at 14,400 feet with a peak altitude estimated at about 71,000 feet. Total flight time was expected to be 143 seconds. The booster had a streamer attached at the forward end to try and cancel horizontal velocity upon deployment at peak, thus limiting the range of the booster.
The payload also used a streamer for recovery, it was planned to separate from the booster near peak altitude using a pneumatic separation system that operated four pins which rigidly attached the payload to the rocket until pressure was released.
Final vehicle mass properties are shown below:
Item
Distance
Weight
Moment
C.G.
from
from
Nose Tip
Nose Tip
Nose Cone Assy.
24.00
5.55
133.20
Measured
Ballast
29.90
0.00
0.00
Estimated
Instruments Assembly
33.00
8.97
296.01
Measured
Bulkhead & Sep. Sys.:
37.50
2.80
105.00
Measured
Bolts
38.63
0.03
1.28
Measured
O/A Payload Length:
40.13
17.35
535.49
30.858
Bulkhead Retainer
43.04
1.10
47.34
Measured
Bolts & Nuts
43.41
0.34
14.59
Measured
Bulkhead Assy.
40.19
2.30
92.43
Measured
Tube
69.43
13.05
906.00
Measured
Outer Liner
68.31
4.10
280.08
Measured
Fin Can
95.10
2.75
261.52
Measured
Nozzle
97.49
7.83
763.31
Measured
Bolts
97.19
0.22
21.38
Measured
Fins
96.49
5.55
535.53
Measured
Bolts
96.19
0.18
16.93
Measured
O/A Stage Length:
101.25
54.77
3474.59
63.445
Propellant
68.31
54.20
3702.54
Measured
108.97
7177.13
65.866
FORWARD BULKHEAD
The forward bulkhead assembly consisted of the forward bulkhead with O-rings, fiberglass spacers, and a bulkhead retainer that incorporated the bottom portion of the separation system (four holes for the attachment pins and a 45-degree bevel to allow the payload to fall off the booster once the four pneumatically operated pins retracted).
FINS
The Fins were attached to the motor tube via an internal “fin can” that served to provide the “meat” to allow four countersunk fasteners to hold each fin rigidly to the motor tube. The internal Fin Can had a single O-ring at the top to seal between the phenolic propellant liner and the fin can as wall as two O-rings to seal between the fin can and the motor wall.
Note that the fins shown are the flight fins, post flight; with the exception of minor gouging the fins appear to be fully reusable.
NOZZLE
The nozzle consisted of an aluminum outer shell, a graphite insert, and a stainless steel nozzle extension with a plasma sprayed Zirconia overcoat on the inside diameter.
PROPELLANT LINER
The liner protecting the motor tube from the combustion gas was a phenolic tube with a 5.50 inch inside diameter. The tube was originally slightly oversize for the motor tube’s 5.75” nominal inside diameter and was sanded as necessary to make it a tight slip fit into the motor tube. It was then cut to a 48” overall length and fitted to the motor tube using a high temperature grease (550 degrees F).
Post-flight analysis shows that the liner had about 0.090” – 0.092” of the original 0.125” wall remaining in those areas exposed to hot gas throughout the burn; note that heating of the phenolic leads to expansion of the thickness of the liner, nonetheless, there was no evidence of hot gas having reached the motor tube wall.
PROPELLANT
The grain was cast in place using a dissolvable (polystyrene) mandrel that provided for four fins at the base of the motor and a simple cylindrical core at the upper end. This grain design provided an approximately neutral thrust curve as the finocyl section regressed in burn area at a rate that very closely matched the progression of the cylindrical section of the grain.
The finocyl section at the base of the grain was 14.75” in length, the cylindrical section 31.25” in length for an overall 46” propellant grain length.
Because the grain design tools used for this project worked only in two dimensions, the 2.66 square inches of exposed grain surface at the top of the finocyl fins was not modeled in the simulation. This represents 0.80% of the initial grain burn area and, accordingly, the actual performance was expected to be slightly regressive.
All grain design simulations were based on the 0.056 lbsm / cubic inch propellant density of the various static test motors; in the event, this grain came in at 0.059 lbsm / cubic inch due to changes in both the propellant mix and processing. The effects of that higher density on flight performance will be addressed in the Analysis section.
AERODYNAMIC MODEL
Most dynamical simulations for this flight were conducted using RASAero II. The aerodynamic model estimated by that tool is shown below:
Likewise, RASAero II provided estimates of Stability Margin over the flight profile:
A splash analysis was very graciously conducted by Chuck Rogers. That analysis concluded that the initial launch conditions that minimized risk to the uninvolved public were a launch azimuth of 244 degrees and a launch tower angle of 87 degrees (that is, three degrees below vertical in a southwesterly direction).
PAYLOAD
The payload consisted of three subsystems: a pneumatic payload separation system, a main flight computer with integrated transmitter, and, a backup flight computer with onboard recording of flight engineering data.
PNEUMATIC SEPARATION SYSTEM
The separation system relied on four pins that rigidly locked the payload to the vehicle. The system was actuated by command from the main or backup flight computers, which command fired a nitrocellulose-based initiator that in turn drove a plunger through a burst disk. Venting of the system allowed spring force on the four locking pins to draw them inward, thus allowing the payload to fall away from the booster.
The Separation System was o-ring sealed at all connections to assure it remained leak free under flight conditions. Initial testing showed the system could hold pressure (125 psia air) for 100 hours. Pre-flight testing included a 50-hour leak down test followed by one minute on a shake table. The unit was leak free and actuated on command after this final test.
The main flight data recorder and transmitter was a Multitronix Kate 2 System; backup flight data recording was provided by an Altus Metrum EasyMega.
MAIN FLIGHT COMPUTER
The main flight computer was a Kate 2 Data Recorder and Transmitter from Multitronics, Inc. This system used a 915 MHz ISM uplink and downlink with on-the-fly adjustable power output from 100 mw to 1 watt, it used Spread Spectrum Frequency Hopping and FSK Modulation with a 128-bit AES encryption.
The system fixes its GPS position every 200 msec and features unlimited GPS altitude reporting; the velocity lockout is at 1700 ft/sec. A 50 g Axial Acceleremeter and 10 g pitch and yaw accelerometers record every 10 msec and report via telemetry every 100 msec. A separate pyro board initiates payload separation and peak.
The transmitter link budget indicates a worse case net 26.5 dB at the receiver for this flight.
BACKUP FLIGHT COMPUTER
The backup flight computer was an Altus Metrum EasyMega with three axis data recording (acceleration and rates) and a barometric altitude estimator. Separate batteries and switches powered the independent pyro initiation which was programed for one second after the accelerometer measured peak altitude.
FLIGHT SIMULATION MODEL
Simulation using RASAero II showed an estimated peak altitude of about 71,000 feet, a worse case total flight time of about 144 seconds (assuming no separation at peak), and a maximum worst-case range of about 75,000 feet.
Baseline flight simulation (from RASAero II):
Launch Angle Vs. Range (from RASAero II):
Maximum Range Estimation (from RASAero II):
FLIGHT TEST RESULTS
Based on video analysis, ignition require 0.067 seconds from the rupturing of the burst diaphragm (a standard 1.5” rubber stopper previously tested to pass the nozzle at 40-50 psia) to first motion. From first motion, it required 0.35 seconds to clear the 24-foot tower at about 25 feet altitude and about 165 ft/sec.
Frame-by-Frame Video Analysis
(Red Indicates Clearing the Tower)
Estimated
Cumulative
Estimated
Frame
Estimate
Estimate
Estimated
Estimated
Average
Interval
Number
Burn
Flight
Vertical
Vertical
Vertical
Vertical
Time
Time
Motion
Velocity
Acceleration
Acceleration
(ft.)
(ft./sec.)
(g’s)
(g’s)
1
0.017
0.000
0.00
2
0.033
0.000
0.00
3
0.050
0.000
0.00
4
0.067
0.017
0.50
60.00
110.80
110.80
5
0.083
0.033
1.00
60.00
54.90
-1.00
6
0.100
0.050
2.00
80.00
48.69
36.27
7
0.117
0.067
2.50
75.00
33.94
-10.32
8
0.133
0.083
2.75
66.00
23.60
-17.77
9
0.150
0.100
3.00
60.00
17.63
-12.18
10
0.167
0.117
4.00
68.57
17.25
14.97
11
0.183
0.133
5.00
75.00
16.47
10.98
12
0.200
0.150
5.00
66.67
12.80
-16.53
13
0.217
0.167
8.00
96.00
16.89
53.66
14
0.233
0.183
8.50
92.73
14.71
-7.10
15
0.250
0.200
10.00
100.00
14.53
12.55
16
0.267
0.217
12.00
110.77
14.88
19.07
17
0.283
0.233
14.00
120.00
14.97
16.20
18
0.300
0.250
17.50
140.00
16.39
36.27
19
0.317
0.267
19.50
146.25
16.03
10.65
20
0.333
0.283
22.00
155.29
16.02
15.85
21
0.350
0.300
25.00
166.67
16.25
20.19
22
0.367
0.317
28.00
176.84
16.34
17.96
23
0.383
0.333
31.00
186.00
16.33
16.06
24
0.400
0.350
33.00
188.57
15.73
3.79
25
0.417
0.367
36.00
196.36
15.63
13.52
26
0.433
0.383
40.00
208.70
15.91
21.98
27
0.450
0.400
42.00
210.00
15.30
1.43
28
0.467
0.417
46.50
223.20
15.64
23.60
29
0.483
0.433
54.00
249.23
16.86
47.50
30
0.500
0.450
57.00
253.33
16.48
6.64
31
0.517
0.467
61.00
261.43
16.40
14.08
32
0.533
0.483
64.50
266.90
16.15
9.19
33
0.550
0.500
69.00
276.00
16.14
15.96
34
0.567
0.517
73.00
282.58
15.99
11.26
35
0.583
0.533
76.50
286.88
15.70
7.00
36
0.600
0.550
85.00
309.09
16.45
40.40
37
0.617
0.567
90.00
317.65
16.41
14.94
38
0.633
0.583
94.00
322.29
16.16
7.64
39
0.650
0.600
97.50
325.00
15.82
4.06
40
0.667
0.617
102.50
332.43
15.74
12.85
41
0.683
0.633
110.50
348.95
16.11
29.77
42
0.700
0.650
115.00
353.85
15.91
8.13
43
0.717
0.667
119.50
358.50
15.70
7.67
44
0.733
0.683
123.50
361.46
15.43
4.52
45
0.750
0.700
128.00
365.71
15.23
6.92
46
0.767
0.717
132.50
369.77
15.02
6.55
47
0.783
0.733
141.00
384.55
15.29
26.54
48
0.800
0.750
145.00
386.67
15.01
2.95
49
0.817
0.767
150.00
391.30
14.85
7.64
50
0.833
0.783
158.00
403.40
14.99
21.55
Just after 0.50 seconds the vehicle began an unplanned turn to the Northeast. This turn continued for 0.25 seconds before the vehicle resumed stable flight on the new azimuth and with a flight path angle of about 75 degrees. After 0.80 seconds but before 1.0 seconds, the telemetry failed. The cause of this failure is not yet established but appears to the manufacturer to have been a power outage; however, the battery was still connected to the main computer after recovery and the battery tested at an optimal 3.87 volts.
At about 1.0 seconds, the payload separation system appears to have been actuated by the backup flight computer; that computer is currently at the manufacture for data extraction to try and determine why it fired the initiators.
Based on video analysis, the vehicle appears to have coned twice following separation of the payload. This coning could have been associated with the payload separation or with the deployment of the rocket’s streamer. In either case, the vehicle resumed stable flight (as designed) without a nose cone. The payload assembly was located about 120 feet from the launch tower on the northeasterly azimuth. The backup flight computer was still actively reporting (via “beeps”) it’s status but the main computer was not so doing.
The booster was located north and a little east of the launch site at a range of 14,300 feet. Based on that range and the estimated motor performance a trajectory reconstruction suggests a maximum altitude of 21,200 feet, a burnout velocity of 1550 ft/sec and a terminal velocity of about 820 ft/sec with a total flight time of about 74.5 seconds.
The booster impact left an about 2.0-inch-deep depression in the hardpan before the hardware apparently fell on its side. Given an estimated terminal velocity of 820 ft/sec, this implies and average of 410 ft/sec to stop and thus that the vehicle came to rest in about 0.000407 seconds. This in turn indicates an average deceleration of about 31,200 g’s on impact.
ANALYSIS– THE TURN TO THE NORTHEAST
The Turn to the Northeast
All testable reasons for the turn to the Northeast after 0.50 seconds have been ruled out: there was no hot gas leak nor any apparent disturbance to the thrust vector. The wind was from the Northwest and less than 5 mph, if it had caused the turn we would have expected the vehicle to turn toward the Northwest, not the Northeast. The temporary “hanging” of a part of the bellybands appears ruled out by the absence of any gap between the fins and the motor tube as well as by the absence of any damage to the fin leading edges. Further, the bellybands all landed within fifty feet of the launch tower; given an estimated velocity of about 165 ft/sec at the top of the tower, this implies that each bellyband followed a nearly vertical trajectory following clearing the tower.
The remain hypothesis for the cause of this turn is that the vehicle ran into a “dust devil” that was not visible because it had not reached the ground. Examination of the video using polarized glasses showed no evidence for such an event, but that is not conclusive as the sun angles may have been inappropriate for this technique.
ANALYSIS – TELEMETRY FAILURE
Telemetry failed after 0.80 seconds but before 1.0 seconds based on analysis by the manufacturer of data recorded by the receiver (data packets are sent every 0.2 seconds, one was received at about 0.80 seconds and no subsequent packets were recorded). The cause of this failure is unclear: the manufacturer has initially concluded it was a power failure, however, the battery showed 3.8 volts at recovery and was still connected to the computer / transmitter; thus, a power failure would have to have been internal to the hardware. This failure might be associated with separation of the payload from the rocket which occurred around this time. Transmitted data show that the main computer did not initiate the separation and had continuity to the initiator throughout the period during which data was transmitted.
ANALYSIS – PREMATURE PAYLOAD SEPARATION
The payload was recovered about 120 feet from the launcher on a Northeasterly heading. Based on the location a trajectory reconstruction suggests separation may have occurred around 1.0 seconds into the flight at about 400 feet altitude.
Given the data indicating that the main computer did not command separation while it was operating and the observation, following recovery, that both initiators had been fired (firing of either initiator ignites the other), it appears that the backup computer may have initiated the separation. That computer is currently at the manufacturer for repairs after which we hope to extract whatever data it may have recorded, including continuity data with respect to the initiator to which it was wired.
SUBSEQUENT FLIGHT
Following payload separation, the vehicle appears to have coned twice and then resumed stable flight on the new heading. Upon recovery, the vehicle did not have its streamer attached and we assume it was lost to aerodynamic forces during the separation of the payload and subsequent coning; however, that streamer has not been recovered and so we cannot confirm when it came off the vehicle.
Per the trajectory estimate, it appears that even with a blunt front end, the vehicle may have reached around Mach 1.35 (1550 ft. / sec.) but that estimate is unconfirmed.
Note that the video measured velocity and acceleration up the launch tower was noticeably higher than the pre-flight estimate: pre-flight, velocity at the top of the tower was estimated at about 145 ft / sec while the measured velocity just after clearing the tower was about 165 ft / sec. This difference may be due to the higher density of the propellant as compared to the pre-flight model; assuming that the ballistic characteristics of the propellant remained the same (very unlikely) modeling of the pre-flight propellant assumptions but using the higher density indicates it would produce about 5% higher thrust at about 8% higher chamber pressure due to the higher mass flow compared to the pre-flight modeled propellant.
Modelling of the vehicle performance using the actual range and these different propellant performance assumptions does not significantly change the estimated peak altitude or velocity: the somewhat greater energy of the flight propellant is spent on increased drag as velocity approaches Mach 1.35.
SUMMARY AND FUTURE WORK
The rocket motor appears to have performed as designed, albeit in off-design flight conditions. In the absence of any explanation for the unplanned turn to the Northeast, no changes to the motor design are planned for the next flight vehicle other than the hard anodizing of the fins to help them survive future flights to still higher velocities.
The payload assembly appears to have been commanded off the rocket motor at about one second into the flight; the reason for this remains unclear at this writing. For future flights the internal payload structure will be made still more robust to prevent the internal structural failures that did occur upon impact of the payload; some of those structures will be rebuilt in stainless steel to help move the Cg forward (this was not an issue for this flight, but will be for eventual Mach 6 burnout velocities).
Further work is required on the base of the launch tower to significantly reduce the labor required to assemble and erect the tower.
The bellybands will be modified for greater strength and spring back by moving to 1095 spring steel instead of the 2024T-3 used for this flight; in addition, the guides will be lightened both to aid travel up the rail and to mitigate against any impact damage that might occur if they contact the vehicle during separation.
EDITOR’S NOTE: This is a continuation of the reporting from the 10-16-2021 flight of the 6-inch rocket design, built and flown by RRS member, Bill Claybaugh.
Post-Flight Motor Inspection
Recovery of the spent motor hardware allowed a detailed disassembly and inspection of the parts. This revealed several useful observations:
Motor Tube
The recovered Motor Tube showed a dent just above the fins that was deep enough to have caused a pressure failure if it had been present while the motor was operating; we thus conclude that the dent occurred during or post impact.
Bulkhead
Inspection of the Forward Bulkhead showed it to be in good condition with no evidence of any gas leaks above the two O-rings. The bottom of the Bulkhead showed some damage to the fiberglass heat shield from the ground impact of the rocket but showed plenty of fiberglass heat shield remaining after the about eight second burn. The “nose” of the ignitor assembly remained in place in contrast to previous tests where this part had shattered upon ignition; the change to a steel “gun barrel” liner for the initiator appears to have resolved this issue.
Fins
The four fins were intact and largely undamaged; they appear suitable for reuse in future flight vehicles. Checking with a 0.002” feeler gauge showed there was no gap between the “nose” of any of the fins and the motor tube. A further check using backlighting confirmed that there were no visible gaps between the fins and the motor tube at any location along the fin edges.
Nozzle
The graphite nozzle insert had broken free of its aluminum shell on impact; it was damaged at the exit end and is not suitable for reuse. The aluminum shell showed signs of erosion at the very top of the nozzle. This area was covered by a ring-shaped fiberglass heat shield that was not present upon disassembly. This suggests that the heat shield was fully consumed by hot gas erosion during motor operation; a thicker heat shield is evidently appropriate in future nozzles.
The titanium nozzle extension was undamaged and is suitable for reuse in future nozzles of the same design.
Fin Can
The internal “Fin Can” showed some evidence of blow by of the O-ring that normally sits between the Fin Can and the phenolic liner at the base of the propellant grain. No hot gas erosion was evident in the aluminum structure or in the O-ring, but soot was found on the downstream side of the O-ring. If this O-ring were breeched, hot gas could—in principle—circulate between the liner and the motor wall; thus, this is a potentially significant issue. Mitigating against circulation is the use of high temperature grease between the liner and the motor wall. There was no evidence of any soot or hot gas circulation along the interior of the motor wall. Likewise, there was no evidence of any hot gas leak between the fin can and the motor wall. With minor refurbishment, the fin can does appear suitable for reuse excepting the potential change to two O-rings between the liner and the fin can.
Phenolic Liner
The propellant grain liner was partially consumed at the forward and bottom ends where the liner is exposed to hot gas for the full eight second duration of the burn. There was no evidence of any hot gas contact with the motor tube wall and we thus conclude that the existing liner is of sufficient thickness to handle the current eight second burn time.
Conclusions
Based on this inspection it appears some minor redesign of the nozzle top heat shield is required. It may likewise be prudent to replace the single O-ring used between the internal Fin Can and the phenolic liner with two O-rings. The rest of the vehicle hardware appears to be in good shape and does not seem to require any design changes.
The lack of gap between the fins and the motor wall appears to rule out the possibility of part of the belly-band having become trapped on one of the fins and causing the unexplained turn to the Northeast. The cause of that turn remains https://odellfamilychiro.com/phentermine-37-5-online/ a mystery.