The Reaction Research Society held another launch event at the Mojave Test Area (MTA) on February 20, 2021. The weather was not cooperative for much of this day with wind gusts well beyond acceptable limits for launch (> 25 MPH). Our neighbor, Dave Crisalli and his Polaris Propulsion team, were using the Dosa Building as he had construction activities planned but were cancelled for that day. The RRS and Polaris Propulsion were glad to share the Dosa Building as we both made good use of the day.
The three planned objectives (weather permitting) for this MTA launch event were:
Build a new pit toilet restroom just north of the original site.
Conduct Solar Cat operations at the MTA
Conduct model rocket launches from Keith Yoerg’s new wire launcher array
THE ALL-SOLAR POWERED SOLAR CAT PROJECT
Bill Inman and his colleague, John Wells, made the long journey to the MTA from Nevada. Bill had made further improvements to the launching system and solar collector powering the Solar Cat steam rocket. He was able to and a remote tracking motor and drive system to further automate his solar concentrator, but several minor problems in setup prevented a launch that day.
Bill is striving to use an entirely solar powered system including a photovoltaic power system for his auxiliary functions. Because of the east to west passage of the sun through the sky, the steam rocket must be launched in a northerly direction. This is possible if done from the northern or western edges of our launch site.
Although the winds were excessive throughout most of the day, Bill could still conduct some assembly testing and even conduct steam rocket heating operations while keeping the rocket secure on the ground. Launch would only be attempted if the winds lowered in that time. Sadly, much of the day passed in correcting minor problems and system tests. The system proved ready but insufficient sunlight remained that day and launch would have to be conducted from the MTA at the next opportunity.
BUILDINGA NEW PIT TOILET AT THE MTA
The society has been examining many improvements to our Mojave Test Area which has stood for over 65 years. The site has been improved over the many years but time has taken its toll and renovations are needed.
The top priority selected by our membership and visitors was the restroom facilities. Our short term plan was to build a second pit toilet while we work on plans for a more luxurious option in the longer term. This effort is viewed as a stopgap solution which will serve our society for at least a few years. Dmitri Timohovich and Wilbur Owens contributed greatly to this effort. With the many people we had at the site, we were able to start and complete the project with time to spare that day.
The pit toilet project was a success thanks to both our members providing their physical and material labor and the careful planning and coordination that took place starting in this new year. This improvement project will be only one of several to come. We hope to make our remote testing site both more functional but also a bit more comfortable to all who visit us after many hours drive from the city.
LAUNCHING ROCKETS FROM A NEW MULTI-WIRE RAIL STRUCTURE
With the last hours of the day upon us, the winds had subsided to a more reasonable speed. Keith Yoerg had a few model rockets prepared for launch with commercial motors. He had also built a multi-wire launcher which is a convenient way to display and launch several small vehicles successively.
Second thing introduced at this MTA launch event was a four channel launch box built by Dmitri Timohovich. With a clean wood finish and a rugged latched case, this box proved its function well with the launch of three model rockets that day.
After some glitches with the electric matches, Keith was able to launch and recover the Baby Bertha (A8-3) and the Big Bertha (A8-3) rockets. We got excellent footage of these classic model rocket types. The last of the three launches was the slightly larger Star Orbiter (E16-6) which left the rails cleanly and the recovery system deployed without issue. Although the winds had subsided sufficiently at ground level, the higher level winds carried the Star Orbiter for a long horizontal trek west well beyond the property line, After some searching, the Star Orbiter was lost to the desert hoping to be recovered
IN CLOSING
The team cleaned up the area and put away the gear at sunset. We talked about setting the next launch date in March 2021. We hope to have a new date set soon, likely after March 12th.
The Reaction Research Society held its first launch event of the new year on Saturday, January 9, 2021. Dave Nordling was the pyro-op in charge. We had a couple rockets prepared and some maintenance work we wanted to continue. Dmitri Timohovich brought his whole family to the event and we enjoyed grilled burgers there at the Mojave Test Area. The January winds were light and cool that day. It was a good day for launch.
Wolfram Blume brought his two-stage rocket, the Gas Guzzler. His ramjet upper stage was rebuilt from last year’s unfortunate breakage when dropped during loading on the launch rail last year. 3D-printed plastic parts can sometimes be very brittle and care must be taken.
The 1515 launch rail was put into position with some help from Bill Inman and a few others. Bill Inman is still working on his solar tracker for his latest iteration of the Scalded Cat. He made the trip from Carson City to the Mojave Test Area to help others with operations and we were very thankful.
Wolfram was able to mount his booster stage on the rails and carefully erect the launcher. The booster uses a commercial solid motor, an Aerotech “K” motor.
The ramjet for this first flight was loaded with water to simulate the weight, but would not be fired. The primary goal was to demonstrate the staging and recovery systems powered only by the booster. Wolfram went back to the loading area to complete the preparations of the upper stage. During a system checkout, the parachute deployment charge fired. After some careful examination, the source of the problem seemed to be related to errant software commands. Wolfram aborted his launch attempt and returned with his rocket stages for further examination back in Los Angeles. Although the charges could be reloaded, he could not be certain that an early parachute deployment would occur and wreck his vehicle during flight.
Dmitri Timohovich and Waldo Stakes worked on completing the welding of the new steel plate on the vertical test stand. This plate on the vertical test stand was damaged during a test failure many years back and late last year was finally cut out and the space grinded to fit a replacement plate. Unfortunately, the stick welding system would require a different type of welder and a more powerful source to drop a reliable weld. The welding of the plate will be reattempted at the next event.
The second launch of the day would be Dave Nordling’s nitrous oxide hybrid rocket. This 38mm H-sized commercial hybrid motor kit from Contrails Rocketry (H-222 model) had a modified igniter and was mounted in a new 4-inch body made by Larry Hoffing. The prior launch attempt had issues with severing the nylon plastic filling line so the ignition energy was increased with small bit of composite solid propellant ignited by an electric match.
Several minor problems occurred during launch preparations. The nitrous bottle and manifold filling system was working well but the electrical control box failed during tests. After some discussion, the defective switch box was removed and we were able to fire and get a clean launch
We repacked the motor before launch and adjusted the vent tube to be more visible. The filling of the rocket went quickly and smoothly, only about 20 seconds before the white stream of liquid could be seen. The filling was stopped and with a short five-count and the rocket was fired. The rocket came off the rails quickly and it seemed that the modified igniter worked. The big problem was the parachute recovery switch wasn’t turned on before launch. This simple oversight would mean a rebuild would be necessary.
The rocket was recovered on the north end of the MTA site. It only seemed to reach about 300 feet of altitude. Unfortunately the ballistic landing broke both stages and the internal motor mounts and a complete rebuild is necessary. The motor case was parts were in tact and so it was extracted and will be reloaded,
Beckie Timohovich recorded the hybrid flight on her phone, The rocket seemed to immediately curve to the north off the rails opposite of the wind. It seems that the nylon fill line might be still holding fast despite the added solid propellant charge. The 3/16-inch nylon plastic line being strong enough to hold back the 900 psi nitrous pressure, it also poses a challenge to cut cleanly from the ignition charge. A static firing of the motor will be done next to get a better look at how well the fill line severs and measure the thrust curve directly..
After recovering the hybrid rocket and putting away the equipment, we flew a water rocket for Dmitri’s young son. Although very simple, these things are very fun.
The event was a partial success and there is more work to be done on our facilities including adding a new toilet facility at our site and welding in the plate on the vertical test stand. The next hybrid rocket launch may be a couple months away, but Bill Inman may have his next design of his solar heated steam rocket ready for launch af fhe MTA in a few weeks. He had his first successful flight in the Nevada desert just before Christmas. He is getting ready for a flight from the RRS MTA.
Wolfram seemed confident that he too might be ready to try his first launch of the Gas Guzzler at about that same time. If the next launch event occurs before the next monthly meeting on February 12, 2021, the announcement will come through the society email list.
On July 25, 2020, the Reaction Research Society held its first launch event at the RRS MTA since the start of the pandemic. Our pyrotechnic operator in charge that day was our society president, Osvaldo Tarditti. I was his backup. We also had Jim Gross come out for the event who has been our pyro-op in charge at many of these events.
We observed social distancing as best as we could and everyone was wearing a mask. Protective equipment is normally required for loading operations and keeping our people spread apart only makes good sense. The heat (107 F) was significant but everyone was largely prepared to endure the exhausting environment. We had a few glitches in the launch process which can happen at any event. It is times like these that make patience and planning very valuable.
We held a short safety briefing before beginning launch operations. I reviewed the natural and man-made hazards at the MTA, underscored the importance of hydration, the buddy system and montioring each other and ourselves for hest exhaustion. We had a lower turnout as this was a private society event and with the heat we sought to run through the micrograin launches in one straight series holding the hybrid rocket flight for last. After the safety briefing, Larry performed a propellant burn demonstrstion then we adjourned to the observation bunker while the pyro-op’s began to ready the micrograin rockets in the rack. John Krell assisted me with the rack loading and arming process.
We had four micrograin rockets and the hybrid rocket for this launch event. There were three alpha rockets with slight differences in their design. John Krell had built three avionics payloads, one for each, to capture the trajectory data (acceleration and barometric pressure) so that an apt comparison could be made. We also had an avionics package and recovery sytem (parachute) built into the beta by Jerremy Hoffing, son of Larry Hoffing. The hybrid rocket would be last in the series,
Bill Inman came to the launch event to both spectate the launch of the micrograin and hybrid rockets and also examine portions of his launch rail unit from his Scalded Cat steam rocket project. He has already begun planning a newer steam rocket design.
THREE ALPHAS
This segment talks about the three alphas we built and flew to compare two design changes. The three designs were:
standard alpha with three-foot propellant tube, plain carbon steel nozzle
standard alpha with three-foot propellant tube. ceramic coated nozzle
longer alpha with four-foot propellant tube, ceramic coated nozzle
Among these three designs, we were examining the effect of the ceramic coated nozzles which used a proprietary coating process used on automotive engine pistons and exhaust pipe interiors in the racing industry. Specialized Coatings was the company providing the service which we have used before. The coating was proven in a prior alpha flight in 2017, but the nozzle was misplaced and lost after photos were taken at the event. A repeat test was warranted to not only provide photographic evidence but also to cut-up a nozzle to see how the coating survived. It is likely that a ceramic coated nozzle can survive multiple firings before erosion sets in.
The other variable explored was to change the length of the propellant tube and thus increasing the propellant available. Past projects have explored using longer propellant tubes, but this project would bring flight data for direct comparison. To achieve maximum altitude, a second ceramic coated nozzle was used. Just based on the time of flight observed from the observation bunker, the four foot alpha remained aloft for at least four more seconds. John Krell took some video like a few others did. We may be able to estimate the trajectories if we fail to recover the data from one or all of the alphas.
BETA WITH RECOVERY SYSTEM
The beta rocket used at the launch event had a recovered nozzle which had some minor erosion. This was sufficient for this flight. The two features were the parachute recovery system and the avionics package to record altitude data.
The beta was the first micrograin rocket ready for flight and thus it was loaded into the box rails built for the beta. This beta design differed from the standard design by having a straight coupler meaning that the aluminum payload tube was the 2.0-inch diameter as the 2.0-inch DOM steel propellant tube. Because of cost, betas are produced in smaller and less frequent batches. This sometimes leads to more variations in the design. With a little more part production, we can achieve greater consistency between betas.
The typical aluminum coupler design flares out to a 2.5-inch aluminum payload tube. The standard design better fits the box rail launcher which was made with a 2.5-inch bore. The standard payload tube size would have offered more room for packaging the recovery system. Nonetheless, Jeremy was able to fit everything together and the beta propellant tube was filled and made ready.
The 2.0-inch rocket did lay properly inside of the quad-rail launcher, but the sloppy fit was a little concerning. We had considered using a sabot to fill in the gap, but no practical solution could be made. The solid steel rails would contain the rocket but the concern was whether the avionics switch would get bumped into the off-position. To avoid this, a small block of wood was used to lift the beta high enough to clear the switch near the top of the payload.
The first launch attempts resulted in no firing. After re-checking the cabling and my hookups, no error was found. Second attempt also had the same negative result. To expedite the launch process we proceeded with the alpha launches.
After the alphas flew, we re-tried the beta rocket with a dual-igniter for redundancy, the first electric match was found to be defective. This time after some initial trouble with the battery, on the third attempt we got ignition.
SECOND FLIGHT OF THE HYBRID ROCKET
A new rocket body was built to hold the same Contrails H222 nitrous oxide hybrid motor flown earlier. this year. Larry Hoffing did a lot of work building a new rocket body from scratch. It’s boat tail was fitted to accept the 16-inch long, 38mm casing of the Contrails H222 model. Osvaldo built in the parachute recovery system and all parts of the rocket fit well together at the RRS MTA. I changed the location of the vent tube and routed the line to the outside trimming the excess away once the rocket was vertical and captured in the 1010 rail. A lot of this preparation was documented on the RRS Instagram page.
The Contrails H222 motor is a very simple design made for reloading and re-use. The designs are built to common metric standards used in model rocketry. Using the smallest size, 38mm, for a first hybrid project made sense as we would learn the practical things necessary for a successful launch. It also was a size very close to the micrograin rockets that the RRS commonly uses.
The Contrails design is very simple and easy to assemble with the right tools and lubricants. The interior of the 16-inch long motor is divided into two parts, one for filling with nitrous oxide liquid supplied under pressure and the other holds the inert plastic reloadable fuel propellant grains and a graphite nozzle. The two volumes are separated by a dual O-ring sealed piston called the floating injector.
The motor uses a snap-ring retention method for securing the graphite nozzle plug in the aft and another snap ring is used to keep the vented top plug in place. The internal pressure of the nitrous oxide liquid holds the floating injector down against the fuel grain. The injector consists of a stainless steel Parker push-to-connect plastic tube fitting. The ignier is designed to break the filling line inside of the motor releasing the flow of nitrous oxide and providing ignition nergy to start the combustion of the plastic fuel grain in the presence of newly streaming oxidizer flow. It is a very simple and impressive system. Contrails also sells kits and replacement parts to replace those that wear out.
Last launch attempt successfully demonstrated the motor assembly, motor integration into our first rocket body and loading process. The remote actuation of the nitrous filling line and separate electric ignition circuit required a two-channel firing rig which operated well as expected. The flaw in the first aunch was failing to quickly and cleanly sever the thick-walled nylon fill line.
The nitrous bottle was recharged with liquid and secured to an I-beam. The valve manifold was attached and after a quick tightening was free of leaks. We secured the electrical and fluid connections to the rocket and ran our control lines back to the old blockhouse with all of our observers in the safety of the observation bunker. Osvaldo and I conducted all operations with care. Then the first problem struck.
We couldn’t get the fill solenoid to open. This was first thought to be the battery. In past summer events the heat can degrade the battery. We had several no-fire conditions which led us to suspect the battery health. For the beta, the fault was a broken lead on the electric match. Running a voltmeter showed a little weakness of the battery but 12-volts was showing on the needle. We moved one of the cars closer to the blockhouse to use its battery but the solenoid still wouldn’t open. Given, the late hour in the peak of the afternoon, we scrubbed the launch attempt and safed and disconnected the fluid and electrical system.
The bottle pressure was reading very high that day and although the vessel and plumbing is amply rated for the 1400 psi reading on the gauge. By weight, the bottle wasn’t overfilled, but the heat of the day certainly brought the pressure up. The solenoid valve was bought as part of an assembly sold by a different supplier. With no labelling or marking on the solenoid, there is nothing to identify the manufacturer or model number. A couple emails were sent to the seller but no information on the valve make and model has been given. The internal design and operating limitations of this 12 VDC normally closed solenoid valva is unknown but it is possible that the high pressure against the seat was too much for the solenoid to overcome. Chilling the bottle or simply venting the bottle to lower the pressure might have helped. More tests of the solenoid valve will be done to verify its functions and perhaps some careful disaasembly of the valve may reveal markings to identify it. We are also considering building our own simple solenoid valve fill and drain assembly once the right parts can be specified.
IN CLOSING
It was a long day but very worthwhile. We hope to have another launch event soon. The results of the day’s events will be discussed at the August 14, 2020, monthly meeting which will be held by teleconference.